I have been a steadfast supporter of
Winnebago. I still believe they are the best motorhome based on value.
But these problems I've had with my generator! Open to the elements, it
suffered from extensive corrosion and became a major maintenance headache.
These problems and photos were documented in 2005. The motorhome,
manufactured in 1997, was eight years old.
Onan need to shoulder a good part of the
blame. Onan's engineering is nowhere near what it should be. Circuit
boards are open to the elements. Connectors are open to the elements.
Wires are free to chafe and burn through. They could have done a much
better job.
Beware ... if you are looking at a Winnebago
be sure to carefully check the generator and the way it is mounted!
Clicking on any photo will give you a
larger image.
The
generator is mounted behind the rear wheels. It is suspended from rails in
a tray.
The generator is not vented through the compartment door.
A cut in the tray allows air to flow in
from the front of the motorhome. This was a HUGE mistake.
In front of the cut-out are the right rear duals. On the road, in
the rain and snow and salt spray enters the compartment and soaks everything.
The spray enters the area where
the brushes press on the stator. All that dirt and salt gets ground right
into the brushes and stator.
Air
also flows around the front of the generator as there is a space between the
door and the generator tray.
If this image is too small, click on it for a
larger image. This is the inside of the control box, behind the front
cover. Notice the pitting and corrosion. Notice the rust on the top
of the starter relay. The whole compartment, and all connections, are a
mess.
The following are specific problems I've
solved.
Aluminum
to Copper Connections Corrode
The generator on my 1997 Winnie, a Onan
Emerald Plus 5000, was producing power. I checked the connections at the
generator's circuit breakers. There was no power at the transfer switch.
The power leaves the generator via some 12 gauge stranded aluminum wire.
That short run terminates in a box where the copper from the motorhome is
attached via a twist connector. I found the problem in the connection
being corroded. It was repaired by using good crimped connections.
In the picture to your right (click on it for
a larger image) a crimp connector has replaced the first hot connection.
Note that the problem is based in the methods
used to mount and ventilate the generator.
Power Wire to Fuel Pump Shorts to Ground
The power wire for the fuel pump is attached
directly to the starter battery lead. That runs unprotected through a
metal hole and to an external fuse and then to the fuel pump. I replaced
the wire with one encased in a plastic tube that will provide more protection
from abrasion. I encased the wire in surgical tubing.
In the picture to the right (a much larger
version is available by clicking on that picture) you can see the battery cable
coming in from your right. A blue wire is attached to the relay connection
and exits the existing hole protected by the tubing. It then goes to the
fuse and then to the pump.
This problem was NOT related to the mounting.
It was simply a poor choice of wire for the job.
Fuel Pump Relay Fails
The fuel pump relay failed. I replaced
it. The original location had the relay buried behind the carburetor and
air intake. The relay was secured to the outside of the generator for
easier access.
In the picture to the right, the relay is
secured to the electronics cover via a stainless steel screw that replaced the
original junky screw.
Again, the mounting is allowing this problem.
This relay should never have failed has the generator been properly ventilated.
New Control Board
Ongoing problems are now pointing to the
control board. That was changed out.
On the old board you can see pitting and
corrosion. I fixed one problem by using a wire to bypass destroyed traces.
The new board shows some differences. The whole board is potted. The
board sits in a type of tray. This means one can no longer check the
component parts. You buy the whole (very expensive) board.
The old board failed due to corrosion.
The last straw was found in shorted windings.
I removed the unit and replaced it.
Generator Removal
Removing the generator was no small trick. I needed to pull it forward and
then drop it down. As it is in the range of 500 pounds, the move had to be
taken seriously. While I might have gone out and bought a transmission or
snowmobile lift, my way worked fine. I built a dolly out of some two-by
material and installed a number of casters to allow for movement. I then
built a second box on top of that one that would allow me to run the generator
for testing. The one side is missing a member as that is where the air is
exhausted. I used two jacks to lift the thing up. My son held one
side, I held the other. My wife pulled the jacks and dolly away from the
motorhome. We then lowered it to the ground. I would suggest using
more jacks, perhaps four. We were concerned about the balance and tipping
using only two.
The original though was to then lift the
generator up and build a workbench from the top box to the ground to allow for
the removal of the dolly. As it turned out, leaving it on the dolly allows
me to run it for testing and still move it to an appropriate cubbyhole for
storage.
If you are buying a Winnie, beware!
Check the generator carefully!
This story continues with the installation of
the new Generac
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